Experimental investigation of a thermosyphon economizer to recover waste heat in the electronics industry
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Date
2020-01-07Author
Yeunyonglul, Pracha
Wongpanich, Somkiat
Watcharadumrongsak, Passwat
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A case study was conducted to design, construct and test a thermosiphon economizer for increasing the temperature of feed water by using waste hot water. The simulation of the thermosiphon economizer (heat exchanger) for the establishment of the optimum size was performed using the thermos-economical method. The thermosyphon was made of a total of 80 copper tubes (outside diam.19.05 mm) with evaporative, adiabatic and condensation lengths of 300, 10 and 300 mm, respectively. The working fluid was R-134a, filling ratio was 50% by evaporative volume, and the thermosiphon was arranged in a staggered form. In testing performance, flow rate of the inlet hot water was set at 10 L/min and the controlled inlet temperature of cold water at 25oC. The average flow rate of the cold water was set at 5, 7 and 10 L/min, respectively. Results showed that the maximum of rate of heat transfer from the condenser section occurred at the flow rate of the cold water of 10 L/min. When test the inlet temperature of hot water of 45,55 and 65 o C were used at the inlet volume flow rate of cold water of 10 L/min maximum heat transfer rates from the condenser 4,626, 8260 and 8,790 W were achieved. Moreover, the outlet temperature of the cold water which was initially 25o C changed to 31,1, 34 and 37o C, respectively. Therefore, increasing the outlet feed water temperature reduced energy consumption. The effectiveness of the thermosiphon economizer with the inlet temperatures of hot water of 45, 55 and 65o C was 0.47, 0.48 and 0.49, respectively.
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